Solving a Coupling Unbalance Problem in the Field

Similar documents
Submerged Pumps and Expanders with Magnetic Coupling for Hazardous Applications

Arrangements of cold exchangers or cold accumulators in cryogenic separation or liquefaction plants.

Bead Roller Operating, Servicing, and Safety Instruction Manual

Introduction of the Design Features of Cryogenic Pumps and Expanders for FSRU Applications

SuperKlean Washdown Products

HVAC Maintenance for DIYers

Steele Extrusion Machinery

CASE HISTORY#1 BAD COOLING TOWER GEARBOX? Barry T. Cease Cease Industrial Consulting (843)

LN series STERLING PUMPS. Horizontal Split Case Pumps. Double Volute. Single Stage.

HEATING AND VENTILATION

Case Study: Preventing Reactor Feed-water 1X Vibration by the Addition of Axial Clearance in the Rotating Assembly

PREVIEW COPY. Compressors. Table of Contents. Introduction to Compressors...3. Lesson Two Reciprocating Compressors...21

specializing in AIR CONDITIONING, PARTS AND SYSTEMS for your classic hi l PERFECT FIT SERIES IN-DASH HEAT/ COOL/ DEFROST FORD TRUCK

AVAILABILITY AND RELIABILITY OF CERN CRYOPLANTS

Experience In Motion. WXH and WXM Utility-Grade Multistage Ring Section Pumps

PERFECT FIT IN-DASH HEAT/ COOL/ DEFROST PLYMOUTH BELVEDERE

INSTALLATION AND SERVICE MANUAL FOR THE TAC1000-P FAN SERIES (PNEUMATIC CONTROL) TAC1000-H FAN SERIES (HYDRAULIC CONTROL)

CASE STUDY ANALYSIS OF CENTRIFUGAL FAN HIGH AMPLITUDE VIBRATION. Ken Singleton

N N O V A T I O N E F F I C I E N C Y Q U A L I T Y

PERFECT FIT IN-DASH HEAT/ COOL/ DEFROST 1968 CHEVROLET IMPALA

CONTENTS. B. System Design and Performance Requirements

All series is using Hitachi scroll compressor, low vibration and high efficiency. Internal thermostat embedded compressors, and it can react quickly.

Commissioning of a 1 MWe Supercritical CO 2 Test Loop

Evolution of Steam Sub-metering at Penn State University

MACHINERY BLOCKING RECOMMENDATIONS

Installation, Operation and Maintenance Manual

Operating instructions

Optimal work climate with open doors. Industrial air curtains Model IndAC

The Digital Scroll Dryer

DBF 4XL Dryer Booster Fans

1 Tan Chek Zin 2 Ng Wei Sing 3 Arni R. Tharakaram. ExxonMobil, Singapore. 4 Satoshi Koguchi Hitachi Japan 1

Goulds 3600 Between-Bearing, Axially-Split, Multi-Stage Pumps. Goulds Pumps

AXUS - SC Short Cased Axial Flow Fans Installation and Maintenance

"S" SERIES IMMERSIBLE PUMP OWNER'S MANUAL INSTALLATION OPERATION PARTS Models S12 S16

High-efficiency Turbo Chiller (NART Series)

Process Simulation and Optimization of Cryogenic Operations Using Multi-Stream Brazed Aluminum Exchangers

Chiller Plant Design. Julian R. de Bullet President debullet Consulting

General Characteristics.3. S.M.A.R.T System Set-up...5. Start-up Procedures.6. Shut-down Procedures 8. General Maintenance..8

Vibration Of Cooling Tower Fans. Barry T. Cease Cease Industrial Consulting Vibration Institute 2015

Installation, Operation, and Maintenance Manual

With the world-renowned SIGMA PROFILE

"S" SERIES IMMERSIBLE PUMP OWNER'S MANUAL INSTALLATION OPERATION PARTS Models S2 S4 S5 SS6 SS7 S8

INSTALLATION AND SERVICE MANUAL FOR THE SERIES 1000-P FAN SERIES (PNEUMATIC CONTROL) SERIES 1000-H FAN SERIES (HYDRAULIC CONTROL) GEN 2

FILLING TECHNOLOGY FROM THE EXPERTS SAFE, CLEAN, POWERFUL

Rambo CAST IRON RING BURNERS OPERATING INSTRUCTIONS. C40LP 3 Ring Burner C50LP 4 Ring Burner

MCF 500 CENTRIFUGAL FAN FOR AIR, FOR BIOGAS, LANDFILL AND NATURAL GAS

Vapor thermocompressor. Stills

A 2 K Active Magnetic Regenerative Refrigeration System for Remote Cooling

PERFECT FIT IN-DASH HEAT/ COOL/ DEFROST FORD PICKUP

AZN ATEX INSTALLATION AND MAINTENANCE

installation manual built-in refrigeration

Installation Instructions Part No , Part No Part No

PhiloWilke Partnership Addendum No. 2 A/E Project No April 2016

Crushing Plant--ZYS High-Efficient Cone Crusher

INSTRUCTION AND MAINTENANCE MANUAL DRYERS A5 - A6 - A7 - A7,5 - A8 - A9 - A10

Air Conditioning Components

A Design for True Performance and Energy Savings In Refrigerated Compressed Air Dryers The Digital Scroll Dryer

CERAMIC PUMPS FGP. Horizontal Liquid Ring Pumps Solid and gas-tight silicate ceramic for gases and vapours.

For Models: DE 441, DE461, DE451, DE490, DC440, DC451, DC490, MRFT415, MRFT440, MRFT460

INSTRUCTION AND MAINTENANCE MANUAL

INSTRUCTION AND MAINTENANCE MANUAL DRYERS A 11 - A 12 - A 13 - A 14 (R410A)

Figure 1. Ejector cross-sectional drawing. Figure 2. Precondenser to left of vacuum flasher. pressure.

Reliability & efficiency without compromise

Montageanleitung RLO (Original) Mounting Instructions RLO (Translation of the original)

Horizontal Split Case Pumps Type U

Copy Right By: Thomas T.S. Wan

LONGONI ENGINEERING SRL

INSTALLATION AND SERVICE MANUAL FOR THE SERIES 2000 & SERIES 3000 FAN SERIES GEN 2

ZETA MAGNETIC AGITATORS

Goulds 3600 Between-Bearing, Axially-Split, Multistage Pumps

PLEASE READ AND FOLLOW THESE INSTRUCTIONS

The Danger signal indicates an immediately hazardous situation which, if not avoided, will result in death or serious injury.

LINDOFLAMM thermal engineering.

Straightening STRAIGHTENING

INSTALLATION AND SERVICE MANUAL FOR THE SERIES 2000 & SERIES 3000 FAN SERIES GEN 1

CERAMIC PUMPS FGP. Horizontal Liquid Ring Pumps Solid and gas-tight silicate ceramic for gases and vapours.

Flygt Top-Entry Agitators CONVENIENT AND EFFICIENT

Rich Knoelke. Questions or Comments: Mulcahy Shaw Water.

PERFECT FIT SERIES IN-DASH HEAT/ COOL/ DEFROST CHEVROLET NOVA

SIZE REDUCTION TECHNOLOGY

CNS CENTRIFUGAL MULTISTAGE WATER DESCALING PUMPS BB4 TYPE API 610 ENGINEERING FLOW SOLUTIONS

(12) Patent Application Publication (10) Pub. No.: US 2014/ A1

PERFECT FIT SERIES IN-DASH HEAT/ COOL/ DEFROST CHEVROLET CHEVELLE/ EL CAMINO NOTE: INSTRUCTIONS DEPICT CHEVELLE

A301 SHOWER PANEL INSTALLATION GUIDE

VIBRA SCHULTHEIS. Vibrating Spiral Conveyors.

Temporary HVAC Equipment, Oil-Free Air Compression and Power Generation

Installation & Operation Manual For ENERGENICS In-Line Space Saver Lint Filters

Zeeco recently had the opportunity

Jaw Crusher. Shanghai Shibang Machinery Co., Ltd

Available online at ScienceDirect. Physics Procedia 67 (2015 )

Mixing Division. Industrial Mixers. MIX S.r.l. MIXING SYSTEMS AND COMPONENTS FOR PLANTS. ATEX RANGE AVAILABLE CM/172

COGEIM COGEIM EQUIPMENT MAINTENANCE AND REFURBISHMENT A NECESSARY CHOISE Number 1 filter-dryer supplier in the world

V SERIES HDR GAS RANGES

Combi Modular System. Standardised centrifugal pumps EN 733 ISO 2858 ISO 5199 API 610

CIRRUS AIRPLANE MAINTENANCE MANUAL

GENERAL 2004 HVAC SYSTEMS. Manual HVAC System - Sorento SPECIFICATIONS. Fig. 1: Air Conditioner Specifications Courtesy of KIA MOTORS AMERICA, INC.

CWS AIR-CONDITIONERS

FAIRBANKS NIJHUIS SOLIDS HANDLING PUMPS.

N N O V A T I O N E F F I C I E N C Y Q U A L I T Y LS BARGE PUMP. Vertical high-flow pump

Monitoring Pump Performance with Vibration. Mitchell Stansloski, PhD, PE

Transcription:

Case Study Solving a Coupling Unbalance Problem in the Field Author: Author: Quraisy A. Shatri P.E. Maintenance Superintendent Machinery and Reliability RasGas Company Limited PO Box 24200, Doha, State of Qatar Tel: (+974) 4492 3209 Mobile: (+974) 5583 8706 e-mail: qashatri@rasgas.com.qa Joseph P. (Joe) Corcoran Manager, Global Services and Training Kop-Flex Emerson Industrial Automation 7565 Harmans Road Hanover, MD USA 21076 Tel: (+1) 410 787 8522 Mobile (+1) 443 831 1811 e-mail: j.corcoran@emerson.com 1

Abstract When a large (3.4 meters long) diaphragm coupling was suspected of causing excessive (120 microns p-p) 1X unbalance vibration between a 90+ Megawatt Gas Turbine and a Propane Compressor in an LNG plant, there was not time to ship the coupling back to a distant factory or service center for troubleshooting. Simple field diagnostic techniques were used to discover the problem, which then led to a field correction and repair so that the unit was able to be quickly restarted with minimum downtime. 2

Process Background In an LNG Plant, After all impurities such as Hg, H2S,H2O are removed in upstream units, sweet feed gas enters the gas chilling & liquefaction unit. Two major pieces of equipment in this unit are the Scrub Column (SC) & the APCI Main Cryogenic Heat Exchanger SC is a distillation column, steam re-boiled, to remove C5+ and provide streams for producing refrigerants (C2 and C3). OH gas of the SC goes in to MCHE mid-bundle for liquefaction. The medium to cool is MR or Multi Component Refrigerant (MCR - C1+C2+C3+N2) 3

Process Background The MR circuit is cooled (and partially liquefied) by Propane. The Propane refrigeration circuit is also tasked to cool Feed Gas in the gas chilling section, De-C2 condenser and the reinjection stream from the refrigerant preparation unit. The two (2) main refrigeration compression circuits MR & Propane are illustrated in the next page. If either of these 2 strings are down, there ll be no production from the gas chilling & liquefaction unit, and no LNG is produced. 4

Simplified schematics 5

Main Refrigeration Compression Strings HM Comp 56 MB Comp 88 M Comp 7 EA Gas Turbine PROPANE #5.5 MSMH-J, Diaphragm coupling rated power 92MW; 3,352.8 mm (Nominal cold shaft separation) HM Comp 56 MB Comp 60 M Comp 7EA Gas Turbine MR 6

RCA The string comprises of 4 coupled rotors: 7EA GT rotor, 88M and 56MB compressor rotors HM rotor Bearings: 3 radial bearings for a single shaft 7EA rotor, 2 radial bearings each of 88M and 56MB rotors, and 2 radial bearings of the HM. Only DE radial vibration of the 88M rotor was extremely high increasing rapidly with increasing speed / load; other bearings-vibe readings were normal. Refurbished 7EA rotor and upgraded (new) 88M rotor were installed during the turnaround. The GT operating data indicated perfect ; factory dimensional and high-speed balance data of the 88M rotor and as-installed records indicated everything was acceptable. Strong suspect was load coupling #5.5 MSMH-J based on possible coupling imbalance as seen via 88M DE vibe plots: new spools & adapter but old coupling-hub were assembled; wrong pre-stretch gap; and poor run-out. Coupling components individual balance records observed to be perfect. On attending the unit, installed couplings run-out checks clearly showed the coupling straightness was grossly out-of- straightness (0.018 ) in mid-span point. Plans to index, change-out of coupling hub was cancelled; previously-installed spacers were re-installed after all necessary checks were done and certified acceptable. Run-out checks of the installed coupling was then checked and certified acceptable for services. The whole string was started-up, sent in to normal operations satisfactorily.

High Vibration Coupling Suspected 8

High Vibration Coupling Suspected 9

Before Disassembling Coupling Installed Runout was Checked -This is Not Normally Done but Can Provide Important Information -Sometimes Difficult to Turn Over Machines -Many Ways to Overcome -Jog Motor (If Motor) -Use Turning Gear -Even Overhead Crane can be Used with Long Strap Wound Around Coupling or Shaft Run Out Should Typically be No Greater Than 0.002 at Flange Connections 0.001 at Hub Bodies 10

Field Installed Run Out Check of Coupling Confirm a Problem 0.45 mm 0.20 mm 0.23mm 0.15mm 0.05 mm 0.03 mm 0.00 mm 11

Next, Previously Installed Coupling was Checked to Reinstall to Get Train Running Is the Available Field Repair Equipment Acceptable? Checked on Calibrated Acceptable Balance Machine Minor Issue w/ Length Capacity of Available Balance Machine 12 Run Outs O K

Then Dye Penetrant Checks of Diaphragms Important Check On Used Diaphragms After Handling 13 No Indications, Cracks, or Unacceptable Scratches

Install Replacement Coupling Center Section o Use Existing Turbine Adapter and Compressor Rigid from the First Coupling o Do a High Spot Check o Line Up High Spots of Male and Female Pilots o Remember that High Spot Definition is the Spot Furthest from the Center of Rotation This Guarantees the Best Balance Condition From a Concentricity to Center of Rotation Perspective

Installed Replacement Coupling Run Out Checks 0.10 mm 0.15 mm 0.10 mm 0.10 mm 0.05 mm 0.10 mm 0.03 mm 0.00 mm No Problem 15

Runout Checks are Good and New Vibration Plots are Good 16

Proof: Vibration Plots are Good 17 Before and After

Proof: Vibration Plots are Good 18

Next - Check of Problem Coupling OK Too!! What is the Problem?? 19

What Could Have Been the Problem? -Installed Run Outs at Positions Other Than Spacer - OK -Mounting Flange and Adapter - OK -Hub Mounting Surfaces - OK -Then we remembered a comment about the difficulty of connecting to the Turbine flange -Re-look at Coupling/Turbine Mounting Surfaces 20

Aha!! ; Clear Evidence of a Mounting Problem Connecting Flanges were not Contacting and were out of Square Even Though Bolts Were Tightened Properly Correct Fit-Up 21 This out of Square caused the Mounted Center Flange High Runout

Recommendations -Improve Existing Turbine Flange Connection for Ease of Assembly -Reduce Width of Guard Pilot -Reduce Amount of Interference at Pilot -Improve Overall Flange Connection Design -Use Standard Design Bolting -Improve Procedure -Leave Coupling Adapter in Place -Handle Diaphragms Gingerly 22

Lessons Learned -If Coupling Balance is Suspected, Check Installed Run-outs -If Replacing Non-Match Marked Components, Find High Spots and Match Them -Dye Check or MPI used and/or handled Coupling Diaphragms -Carefully Handle any Diaphragm - Do not lay face down on rough surface -Understand Installation Potential Difficulties When Designing Coupling 23