PETROKEMYA (SABIC) Control Loop Performance Monitoring and Assessment

Similar documents
2012 Honeywell Pacific Users Group. Sus tain.ability.

Diagnostics with fieldbus

INSTRUCTION MANUAL FOR MICROCOMPUTER BASED TEMPERATURE INDICATING CONTROLLER JCD-13A, JCR-13A

Advanced Diagnostics for HART Protocol Rosemount 3051S Scalable Pressure, Flow, and Level Solutions

Overcoming the Challenge of Implementing Profit Controller on a Third Party DCS. Ramiro Andrés Cremaschi Julia Alejandra Perinetti Repsol YPF

C&I SYSTEM DIAGNOSTICS WITH SELF MONITORING AND REPORTING TECHNOLOGY (SMART)

ADVANCED MONITORING AND DIAGNOSTIC SYSTEMS FOR INDUSTRIAL GAS TURBINES

Q&A Session from Alarm Management Workflow Webinar (Apr.24/2013)

White Paper. Integrated Safety for a Single BMS Evaluation Based on Siemens Simatic PCS7 System

Critical Condition Management on a Corporate Scale. Lyondell Is a Major Global Chemical Company

Temperature + Humidity (%RH) Control & Recording System with 8 / 16 Channel Mapping. Touch Panel PPI

INSTRUCTION MANUAL FOR MICROCOMPUTER BASED TEMPERATURE INDICATING CONTROLLER FCS-23A

Improving the Performance and Reliability of Fired Heaters and Boilers

Enhance Alarm Management

excellence in Dependable Automation ALARM MANAGEMENT

CombustionONE. Improving and Sustaining the Combustion Asset. Driven by the New Standards. Bulletin 53A90A01-01E-A

Smarter Field Instrumentation Life Cycle Management. Ray Rogowski Global Marketing PMC Instruments

Sustainability in commercial laundering processes. Management Systems

Recovery Boiler Advisor

Process Safety - Market Requirements. V.P.Raman Mott MacDonald Pvt. Ltd.

DATA SHEET BENEFITS CURRENT CHALLENGES SSM INFOTECH S X-FORCE AMS - THE IDEAL SOLUTION

DeltaV Analyze. Introduction. Benefits. Continuous automated DeltaV System alarm system performance monitoring

Temperature Control of Heat Exchanger Using Fuzzy Logic Controller

Operational Overview and Controls Guide

Advanced HART Diagnostic Suite

Product introduction Layers of Protection Layer 3: Safety System Instrumented & Mechanical. Layer 2: Alarms Manual action needed

Failure Modes, Effects and Diagnostic Analysis

Improved Dryer Control

ARTIFICIAL INTELLIGENCE TEMPERATURE CONTROLLER

Speed and Frequency Seite 1 von 7

DynAMo Alarm & Operations Management

UDC1000 and UDC1500 MICRO-PRO SERIES UNIVERSAL DIGITAL CONTROLLERS

CONTROLLING BOILER SWELL AND SHRINK

Ovation Alarm Management System

INSTRUCTION MANUAL FOR MICROCOMPUTER BASED TEMPERATURE INDICATING CONTROLLER GCD-200, GCR-200

UDC100 Universal Digital Controller Specifications

Figure 1. Ejector cross-sectional drawing. Figure 2. Precondenser to left of vacuum flasher. pressure.

2012 Honeywell Users Group EMEA Tyron Vardy A Guide to Effective Alarm Management

Green Energy Engineering, Inc.

Alarm Management Services

VT4810 SINGLE / DUAL ZONE CONTROLLER INSTALLATION MANUAL

Sustain.Ability. Alarm Management: Be Pro-active, not Re-active Honeywell Users Group Europe, Middle East and Africa. Tyron Vardy, Honeywell

DON T JUST REPORT ON ALARMS, TAKE

Nov 08 PRODUCT SPECIFICATION SHEET

Condition monitoring using FAG products. Technical Product Information

EXPERIENCES OF REDUCING STEAM CONSUMPTION IN A SUGAR PLANT

L automazione al servizio della manutenzione

Real Time Pipeline Leak Detection on Shell s North Western Ethylene Pipeline

opti-visor ultra-efficient chiller plant automation Typical specification

Stavros Chrysanthou Madrid DynAMo Alarm Management Secrets to unlocking complete Operational Integrity

CONTROL SYSTEMS Combustion Control Burner Management Control Balance of Plant Equipment Control Supervisory Control and Data Acquisition

AVOID CATASTROPHIC SITUATIONS: EXPERT FIRE AND GAS CONSULTANCY OPTIMIZES SAFETY

All DC Inverter Multi VRF

PROCESS CONTROL COURSES

Alarm Management. Version Prepared by: Michael Davis- Hannibal. Softcon Software Control Services (Pty) Ltd.

ENERGY LIGHT USER S GUIDE ENERGY LIGHT USER S GUIDE

AVOID CATASTROPHIC SITUATIONS: EXPERT FIRE AND GAS CONSULTANCY OPTIMIZES SAFETY

L automazione al servizio della manutenzione nell industria di processo

Refrigeration Controller Operator s Manual (HRC) PO Box 6183 Kennewick, WA

For Complete Fire and Gas Solutions

Brine Generation Study

Retrocommissioning Findings Summary: Building X #1 Priority: Major Comfort/Control Problems

Perimeter Product Overview. Effective protection for your business

I&C Upgradation and Modernization at CHASNUPP 1 & 2. Presented By: Waseem Uddin Farooqi PAEC, Pakistan

INSTALLATION INSTRUCTIONS

Product Specification

Continuous Commissioning: A Valuable Partner to Retrofit Projects

Dynamic Simulation of Double Pipe Heat Exchanger using MATLAB simulink

Table of Contents PART I: The History and Current Status of the Industrial HMI PART II: Fundamentals of HMI Design and Best Practices

Kevin Brown and Chris Stearns

Burner Management and Combustion Control. Copyright 2014 Rockwell Automation, Inc. All Rights Reserved.

STEAM STERILIZER SERIE S1000 (RBE)

STEAMPAK Series BurnerPAK BMS Burner Management Systems

Refrigerated Compressed Air Dryer

DeltaV Operate. DeltaV Operate. Introduction. DeltaV Product Data Sheet. Robust and secure plant operations

AUTOMATION OF BOILERS USING LABVIEW

PREVENTIVE PROTECTION PROTECCIÓN PREVENTIVA

Workshop on AFDD for RTUs Moving from R&D to Commercialization July 13, Introduction

DIRECTIVE NO: D-B

DYNAMO ALARM MANAGEMENT

Datasheet Crowd Management

NC NC Series. NG Series. Seresco s NG Series Fluid Coolers & NC Series Outdoor Condensers Quiet, efficient reliable heat rejection

Certification Report of the ST3000 Pressure Transmitter

Non-contact voltage (for SSR drive): V DC DC current: 4 to 20mA DC Thermocouple: K, J, E Input. RTD: Pt100, JPt100

Certification Report of the ST 3000 Pressure Transmitter with HART 6

MEDICAL CHILLER SYSTEMS

Owner s Manual Super-Slim Four-Way Cassette

Advanced Autoclave Controller with Recording + 4 Channel Mapping + Pressure Indication with PC Software & Printer Module

Miniature Thermoelectric Cooler Controller MTCC-01 user's guide

INSTALLATION INSTRUCTIONS FOR SERIES 9 INTERMITTENT PILOT IGNITION CONTROL

ENERGY OPTIMIZATION IN THE MAA GAS PROCESSING FACILITIES

INSTALLATION INSTRUCTIONS

DigiTrace NGC-family

Controllers, Indicators & Set Point Programmers

MultiPlex INNOVATIVE COMPRESSED AIR SOLUTIONS LARGE CAPACITY TRUE-CYCLING TM REFRIGERATED COMPRESSED AIR DRYERS

Bench Mark 6SigmaET Thermal Simulation Software

Integrated Automation Instrumentation & Terminal Devices

Healthy. Atmosphere. for Pigs and Poultry. for a

TEMPERATURE CONTROL MODULE MODEL R3-TC2

INSTALLATION, OPERATING & MAINTENANCE INSTRUCTIONS FOR 870 SERIES INDUSTRIAL CONTROL PANELS

Transcription:

PETROKEMYA (SABIC) Control Loop Performance Monitoring and Assessment Presentation at KFUPM Monday, 24 th November 2008 Petrokemya Olefins-III by Khalid T. Al-Ruwaili Manager, Control System Department Petrokemya, SABIC v

Contents Introduction The incident Study objectives Study findings Solution & Decision i Project implementation Benefits 2

Introduction When it comes to performance of Control Loops in Process Industries, it is said that the day plants were built, it started to go bad. With continuous operation, wear & tear, material variation, seasonal changes, and changes in process characteristics, plants drift away from their optimal performance. Most industries realize it only after a big process upset or production loss. 3

The incident In Olefins-II, the VHP to HP steam-let-down valve PV-8660 had problems since plant startup. So, Operations kept the valve in MANUAL mode, as its performance in AUTO mode was not satisfactory. When the Process Gas Compressor (BK-0201) tripped on 31st December 2004, VHP Steam demand came down, and because PV- 8660 got stuck at 20%, HP steam header pressure dropped. This reduced turbine speed of BFW pump and caused lack of BFW, and in turn eight (8) millisecond furnaces tripped. Olefins-II plant was down for 16 hours, and total production loss was equivalent to 3680 metric tons of ethylene (SR 5, 851,200). 4

Study objectives Main objectives of the CSD survey were, To study the reasons for performance-deterioration of control loops over a period of time, due to which control loops in various plants of Petrokemya were kept in MANUAL mode, and not in their DESIGN MODE of operation. To develop a system and apply the latest hardware / software tools to study, monitor, and improve the performance of critical control loops, on a continuous basis. 5

Study findings Control Loops working alright, but may deteriorate anyway Change in the process characteristics Operations prerogative Control Valve problems Inadequate control scheme design Other reasons 6

Study findings (cont) Category Description Controllers status VCM Plant PVC Plant PPS Plant lyethylene Po Olefins-I Olefins-II Olefins-III Utilities Overall 1 2 Controllers apparently working alright but may deteriorate anyway Change in process characteristics Auto 279 470 87 0 532 829 989 159 3345 Manual 9 5 9 0 16 21 2 5 67 3 Operations prerogative Manual 25 26 12 0 20 464 101 7 655 4 Control Valve problems Manual 3 4 4 0 8 3 4 2 28 5 Inadequate design Manual 8 4 0 0 0 3 47 3 65 Total per Plant 324 509 112 0 576 1320 1143 176 4160 Loops on Auto: 3345 (of 4160) Loops on Manual: 815 (of 4160) 7 7

Control Loops working alright but Control loops are tuned during plant initial commissioning PID parameters are set based on experience Problematic control loops are tuned through trial and error Plants may run for their lifetime with sub-optimal controls Control valves become mechanically deficient Flow control valve does 1-2 million reversals/year Valve packing frequently over-tightened to prevent emissions Causes valve stiction and control loop cycling Process characteristics change with time Equipment fouling, wear, modifications Even well-tuned control loops develop problems 8

Control Loops working alright but (cont) Limit of Operability Alarm Limit Reduction in benefits Lowering of set point to maintain safety margin Variability increases over time Reduced Profit Running further from Constraints Increased Maintenance Costs Equip & Valves Cycling Increased Operator Loading Alarms, Intervention reqd. After optimization 9 Performance decreases over time 2 3 years later 9

Control Loops - symptoms of poor performance Excessive variance Oscillatory behavior Disclosing events Increased alarm frequency Operator intervention ti Loops placed in manual mode Controller output saturation Excessive Variance Oscillatory Behavior Frequent alarms Operator intervention PID Tuning changes Loop in manual Output runs into limits Poor Control Loop Service 10

Change in the Process Characteristics Compared to the original design, process characteristics change with time. Plant modifications, equipment wear & tear or fouling and varying plant loads, contribute to deterioration in the performance of control loops. For example, Plants are modified, debottlenecked, or added with new equipment In VCM plant, guided wave radar level instruments were identified and successfully used as a replacement for obsolete and problematic displacer type level instruments. In Olefins-I, nearly 56 VORTEX flow meters are installed in place of Orifice plates in furnace dilution steam flow meter applications, to overcome problems like, frequent plugging of impulse tubing with coke particles, and unstable & oscillating flow measurement. 11

Operations prerogative Over a period of time, plant operating personnel develop opinion on some control loops that there will be problems irrespective of the actions they take. Or, the Operators do not keep some control loops in their designed MODE of operation due to other reasons. For example, In PVC plants, 15 Poly Reactor pressure control loops are in MANUAL mode, against their designed AUTO mode, to avoid releasing VCM to atmosphere. 12

Control Valve problems Hysteresis Stiction Nonlinear Installed Characteristic Oversized Control Valve These problems cannot be solved through tuning Hysteresis Stiction Non-linear characteristic Oversized valve 13

Inadequate Control Scheme design Process units or equipment are provided with inadequate control schemes to control them, or inadequate field instrumentation to measure the required process variables. When it comes to performance of control loops, it becomes very difficult to judge, whether adequate control schemes are provided in the first place. For example, When we compare three ETHYLENE plants in Petrokemya, which were built at different times, the number of control loops and field instruments t in each ethylene plant kept increasing i significantly. ifi 14

Solution & Decision In the first phase of the project, we decided to go in for the following, Control Loop Performance Monitoring and Assessment package Control Loop Tuning package Alarm Management System (AMS) package And, in the second phase, we plan to go in for the following, Plant-wide Advanced Process Control Real-Time Optimization 15

Project implementation (Olefins-II) We decided to implement the project in Olefins-II first. We prepared Invitation-To-Bid (ITB) documents and sent them to renowned Automation Companies. After technically and commercially evaluating the proposals, we selected the solution offered by Honeywell for Olefins-II. Deliverables, Loop Scout OperTune Alarm Scout Advanced Alarm Management (AAM) Alarm Configuration Manager (ACM) Alarm and Event Analysis (AEA) User Alert (UA) Loop Scout Server, Advanced Alarm Management (AAM) Server PowerEdge 1800, Xeon 3.0 GHz, Dual CPU, SATA Raid-5 hard disk 16

Project implementation (VCM) Then we moved on to Vinyl Chloride Monomer (VCM) plant. This time, we selected Process Automation Systems (PAS) after technically and commercially evaluating the proposals from renowned automation companies. Deliverables, ControlWizard TuneWizard Alarm Analysis Module Alarm Documentation and Rationalization (D&R) module Automatic Data Update (ADU) module Real Time Alarm Management Application PlantState Suite Server DELL tower, Xeon 3.0 GHZ, Dual CPU, 4GB SDRAM memory, 73 GB Raid-5 hard disk 17

Project implementation (VCM) Internet Clients External Firewall Business LAN Controller Performance, Controller Tuning, Alarm Management Servers Internal Firewall Process Control Network OPC DA Server Clients DCS 18

Project implementation (VCM) ControlWizard Treemap Performance Display provides a visual overview of loop performance, loop importance, and draws attention to problem areas. Assessment Details viewer shows data used for analysis, lists statistics, and provides corrective actions 19

Project implementation (VCM) Assessment Details viewer shows data used for analysis, lists statistics, and provides corrective actions. Advanced Assessment Details viewer provides autocorrelation, impulse response, and power spectrum plots, as well as detailed results of performance analyses. 20

Project implementation (Olefins-III) Too many alarms causing nuisance Many alarms were disabled (process safety) History Module (HM) of Honeywell DCS overflowing Difficult to retrieve alarm history of last few hours 12 % - BADPV alarms Null reading for fraction of a second. Mainly temperature alarms/defective thermocouple 30 % - OFFNORM alarms Change of state Deluge valve Pump seal leak Burner scanner failure 21

Project implementation (Olefins-III) 55 % - PVHI and PVLO alarms Process value exceeding high/low alarm limits Wrong selection of alarm limits Poor controller tuning Varying feedstock Controllers were tuned by Honeywell Alarm limits were corrected based on feedstock Dead bands were created to allow for process swing Time delay was provided for process swing. Bad PV alarms were removed for temperatures 22

Project implementation (Olefins-III) Olefins-III NUM MBER OF ALARMS P ER HOUR 42 Journey from Overloaded Workstation to Robust" Workstation % PLANT UPSET 23

Benefits Continuous monitoring of all loops Automatic assessment Non-invasive Provides an overview of all loops Prioritization of maintenance efforts Problem identification & diagnosis Scheduled reporting Maintain Advanced Process Control benefits Typically, 40-70% of savings from APC projects are achieved by optimizing the performance of control loops Reduce frequency & severity of abnormal situations Poor performance of control loops contribute to 30% of preventable/unplanned plant downtime 24

Benefits (Cont) In Olefins-III, We achieved 93% reduction in total alarms per day (from 52,000 to 4,000 for 4 workstations). We moved from "overloaded" workstation to "robust" workstation. We achieved this within 7-weeks of installing the system. Operators are now able to concentrate ce on process related issues better than before. Nearly 95% of control loops run in their designed MODE. We achieved stable operation of C2-splitter splitter, and overall production increase of 3% (Capacity of the plant is one (1) million-tons-per-year of ethylene). 25

Thank You Any Questions? Khalid T. Al-Ruwaili Manager, Control System Department 26