DATE: 2/29/2012 DAILY WORKOVER / COMPLETION REPORT ISO. 3 loads of lime stone and leveled off. Re-spot 2-3/8" used tubing. VAC TRUCK FISHING TOOLS

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1 DAE: 2/29/2012 DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI ACK HOE WORK PERFORMED A- ANCHOR tart ime:0:am top time: 0:00 pm - ROUAOU C- UPERVIOR D- REVERE UNI JRC ackhoe, Cleaned up location and leveled off the well area. pot E- OP' 3 loads of lime stone and leveled off. Re-spot 2-3/8" used tubing. VAC RUCK FIHIN OOL Andrew Anchor, Checked perm anchors on location, OK. WIRE LINE E Waiting on Workover rig and AFE approval. Will spot Reverse unit tomorrow to flow the into. DAILY CO 0 ACCIDEN: -0- PREVIO CO 0 REPOR Y: Hadi OAL CO 0 RI# PHONE: RIPLE N WELL# 124 h 36 h L.Penn cast iron bridge plug@9412' 12500' 12594' Ellenberger formation Hadi 2/28/2012 D: 12600'

2 DAE: 3/01/2012 h DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI ACK HOE WORK PERFORMED A- ANCHOR tart ime:0:am top time: 0:00 pm - ROUAOU C- UPERVIOR High wind and sand storm after noon. D- REVERE UNI Moved in and unloaded" Hinton "Reverse equipment on location. E- OP' asic ervice rig arrived on location. hut down due to high wind VAC RUCK FIHIN OOL Waited on orders and AFE approval to work on the well. WIRE LINE E DFN. DAILY CO 0 ACCIDEN: -0- PREVIO CO 0 REPOR Y: Hadi OAL CO 0 RI# PHONE: RIPLE N WELL# PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

3 DAE: 3/12/2012 Monday DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 1450 asic -A ACK HOE 350 JRC - WORK PERFORMED A- asic well service 1450 provide service rig REVERE UNI 1450 Hinton -C tart ime:1:pm top time: 6:00 pm - JRC 350 dug dirt pit UPERVIOR 0 Hadi -D C- Hinton 1450 provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Drove rig to well location. hut well in. D- Hadi 0 supervise operation & fishing Dope and valve 0 Produ. pecial -F Held safety meeting with crew. Lock and tag Electric ox. E- Andrew pump 0 Pump repair OP' 300 Cavaloz - Disconnect flow line from casing and tubing string. Leveled off location F- Prod. pecialty 0 Pipe dope, valves, wood seals VAC RUCK around the wellbore area. - Cavaloz 300 provide bop stack. Rigged up asic rig, tied guy line to perm anchors on location. Rigged up Hinton Reverse unit Already tand by on location. Un-beamed head, Laid down H.head. PU and unseated pump, Laid down polished rod and ponny rods off the ground. Closed well in. DFN. DAILY CO 3,550 ACCIDEN: -0- Daily Cost: $3,550 PREVIO CO 0 REPOR Y: Hadi C.Cost $3,550 OAL CO 3,550 $3,550 RI# PHONE: RIPLE N WELL# PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

4 DAE: 3/13/2012 U DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3845 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:1:pm top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Continued pooh w/ tapered rod string, standing back 116-7/8" rods, 127-3/4" D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F rods,and laid down 111-5/8" rods, and 12 sinker bars in singles. E- Andrew pump 0 0 Pump repair OP' 0 Cavaloz - F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 270 ejas -H Nipple down wellhead flange, Released AC. Nipple up bop's. tart out - Cavaloz provide bop stack. hole with 2-3/8" tubing. Pull and laid down 104 joints of 2-3/8" tubing in H- ejas Vac rucks 270 huling water to rev pit. singles. pot 12/12"x20' seals and closed wellbore in. DFN. Will continue DAILY CO 6,365 AFE $ ACCIDEN: -0- Daily Cost: $6,365 PREVIO CO 3,550 REPOR Y: Hadi C.Cost $9,915 OAL CO 9,915 $9,915 RI#1215 PHONE: RIPLE N WELL# PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

5 DAE: 3/14/2012 wd DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3080 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:1:pm top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Cont'd pulling 2-3/8" tubing and laid down in singles. Pull and laid down D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F total of 238 joints of 2-3/8" tubing. ubing Anchor hung up and could E- Andrew pump 0 0 Pump repair OP' 0 Cavaloz - not pull tubing. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Work tubing, pumped 50 bbl of water down casing unable to pull - Cavaloz provide bop stack. tubing coming out. Anchor is free and would go down the hole but H- ejas Vac rucks huling water to rev pit. hungs up coming out hole( could have an object on top of anchor or one of slips came loose keeping the tool from coming out) Closed well in. Called office for pipe recored they have only 1988 pipe record) will log to find out how may joints of tubing in the hole and plan to cut tubing ahove tubing anchor. DAILY CO 5,330 AFE $ ACCIDEN: -0- Daily Cost: $5,330 PREVIO CO 9,915 REPOR Y: Hadi C.Cost $15,245 OAL CO 15,245 $15,245 RI#1215 PHONE: RIPLE N WELL# PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

6 DAE: 3/15/2012 h DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3660 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:1:pm top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E hick fog this am, fog lifted at 9 am. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Continued working 2-3/8" tubing with ubing anchor while waited on E- Andrew pump 0 0 Pump repair OP' 0 Cavaloz - Rotary wire line unit to sever the pipe. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Worked anchor 45 minutes, moving 2-3/8" up the hole with drag. - Cavaloz provide bop stack. WIRE Line 2000 Rotary -I Finished pull and laid down tubing and tubing anchor complete. H- ejas Vac rucks huling water to rev pit. All the parts on tubing anchor came out hole. Finished pull out hole with I- Rotary wire line tand by to cut pipe. 284 joints of 2-3/8" EUE 8rd tubing ( in good condition) 7" ubing anchor catcher 15 joints of tubing eating Nipple with mule shoe assy. otal of 299 jts 2-3/8" tubing. Made up and attempt to run 6-1/8" mill and 6-1/8" shoe would not pass 10' below the wellhead. Checked drift with 6-1/8" bit went through. Unload 57 joints new 2-7/8" tubing on location. IH with tbg open ended while waiting on wash pipe. Closed well in. DFN. Will continue DAILY CO 7,910 AFE $ ACCIDEN: -0- Daily Cost: $7,910 PREVIO CO 15,245 REPOR Y: Hadi C.Cost $23,155 OAL CO 23,155 $23,155 RI#1215 PHONE: RIPLE N WELL# ok PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

7 DAE: 3/16/2012 Frid DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 1450 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 2:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Waited on Hadi urn down mill. Made up and IH with 6" od stablized mill D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F on 2 drill collars, and 72 joints of new 2-7/8" L80 tubing. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Closed well in and waited for new work string to arrive. Received call F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H that new work string can not be delivered until Monday morning. - Cavaloz provide bop stack. WIRE Line 0 Rotary -I H- ejas Vac rucks huling water to rev pit. DFN. Waiting on new work string. I- Rotary wire line tand by to cut pipe. Will resume operation Monday. DAILY CO 3,750 AFE $ ACCIDEN: -0- Daily Cost: $3,750 PREVIO CO 23,155 REPOR Y: Hadi C.Cost $26,905 OAL CO 26,905 $26,905 RI#1215 PHONE: RIPLE N WELL# ok PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

8 DAE: 3/19/2012 Mond DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3600 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 2:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E ruck load of work string arrived on location. ucker Forklift unload D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F 243 joints of 2-7/8" EUE 8rd tubing. Check and measured tubing string. E- Andrew pump 0 0 Pump repair OP' 100 Cavaloz - F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Cont'd ih with 6" mill, pick up tubing off the ground. agged bottom at - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I 9372' with 300 joints of tubing. H- ejas Vac rucks huling water to rev pit. VAC RUCK Once ource -J I- Rotary wire line tand by to cut pipe. 2-7/8" U DRM -K Rigged up swivel, pumped 100 bbl of fresh water down to circulated well, J- Oneource Vac 0 0 hauled water to rev.pit no circulation. Closed well in. K- DRM pipe co /8" tubing DFN. DAILY CO 5,950 AFE $ ACCIDEN: -0- Daily Cost: $5,959 PREVIO CO 26,905 REPOR Y: Hadi C.Cost $32,855 OAL CO 32,855 $32,855 RI#1215 PHONE: RIPLE N WELL# ok PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

9 DAE: 3/20/2012 U DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3600 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. " Well On Vac" C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Unload 100 jts of 2-7/8" new tubing from DRM pipe supply co. Forklift same. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F check and inspected tubing. Ok. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Rigged up swivel, tagged at 9372' attempt to circulate well. Well on vac. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H lost 450 bbl while attempting to get circulation. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I Lowered mill and start milling at 9372' (plug at 9412') H- ejas Vac rucks huling water to rev pit. VAC RUCK Once ource -J Milled on joink and cmt from 9372' to 9402' with no circulation. Work and I- Rotary wire line tand by to cut pipe. 2-7/8" U DRM -K rotate string. J- Oneource Vac 0 0 hauled water to rev.pit Operator picked up tubing with torque, tubing made several back spin to left K- DRM pipe co /8" tubing may caused to back off drill collars. Laid down swivel, and start out hole with 40 joints tubing to check HA. Closed well in due to high wind. otal water lost in the hole 1220 bbl. No circulation. ejas and one-source hauling water loc. DAILY CO 5,900 AFE $ ACCIDEN: -0- Daily Cost: $5,900 PREVIO CO 32,855 REPOR Y: Hadi C.Cost $8,755 OAL CO 38,755 $38,755 RI#1215 PHONE: RIPLE N WELL# ok PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

10 DAE: 3/21/2012 Wd. DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 2800 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 4:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. " Well On Vac" C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Finished pooh with tubing and HA, Checked drill collars, OK. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F checked mill worn down due to loose junk on top of cement and plug. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Cleaned up mill recovered ridge plug slips, and hand full of rubbers. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I Ex-changed mill with 6"mill and start in hole on 2 drill collars. agged tight H- ejas Vac rucks huling water to rev pit. VAC RUCK Once ource -J tight spot in casing at 1796'. Pulled 20k over to pull loose. I- Rotary wire line tand by to cut pipe. 2-7/8" U DRM -K Pooh with tubing and laid down mill. ent mill to shave & trim down. J- Oneource Vac 0 0 hauled water to rev.pit Closed well in. DFN. K- DRM pipe co /8" tubing Dry drilled to 9412' DAILY CO 5,100 AFE $ ACCIDEN: -0- Daily Cost: $5,100 PREVIO CO 38,755 REPOR Y: Hadi C.Cost $43,855 OAL CO 43,855 $43,855 RI#1215 PHONE: RIPLE N WELL# ok PD: what is here Reported PD@9375'!!!??? junk??!! cast iron bridge plug@9412' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

11 DAE: 3/22/2012 h DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3600 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 5:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. " Well On Vac" C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Made up re-dressed 5-7/8" Hadi's bladed mill on 2-7/8" new work string. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - rip in hole with mill, on 303 joints of tubing. agged ridge plug and junk F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 850 ejas -H at 9412'. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I RU swivel, milled on ridge plug and junk without circulatio (well on vac at H- ejas Vac rucks huling water to rev pit. VAC RUCK Once ource -J 3 bbl/mt) Mill and drilled on plug 40 minutes broke loose, and continued I- Rotary wire line tand by to cut pipe. 2-7/8" U DRM -K picking up tubing and drilling down. J- Oneource Vac 0 0 hauled water to rev.pit VAC RUCK 750 M.VAC -L Cleared casing from 9412' to without circulation. While going in the K- DRM pipe co /8" tubing hole driller noticed a problem with the rig. hut down operation. L- M.Vac trucks hauled water to rev.pit (Found two broken spots on the beam holding draw works) put 80 bbl water down casing. Closed wellbore in. otal vol of water lost in the hole: 1820 bbl. asic will make rig repair or change the rig. DAILY CO 7,500 AFE $ ACCIDEN: -0- Daily Cost: $7,500 PREVIO CO 43,855 REPOR Y: Hadi C.Cost $51,355 OAL CO 51,344 $51,344 RI#1215 PHONE: RIPLE N WELL# ok drilled to 11339' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

12 DAE: 3/23/2012 Frid DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12499'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 0 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Re-arranged work string tubing, and cleard location. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Checked well and prepared "Hot work Permit". aisic Energy welded E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - broken frame on the rig. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H IH with 127-3/4" and 116-7/8" rods off derrick. Hung rods with plished - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I rod calamp. H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J rig down asic rig 1215 and moved rig off location. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K Closed well in. J- Oneource Vac 0 0 hauled water to rev.pit VAC RUCK 0 M.VAC -L DFN. K- DRM pipe co /8" tubing L- M.Vac trucks hauled water to rev.pit Eot@ 11339' otal vol of water lost in the hole: 1820 bbl. DAILY CO 2,300 AFE $ ACCIDEN: -0- Daily Cost: $2,300 PREVIO CO 51,355 REPOR Y: Hadi C.Cost $53,655 OAL CO 53,655 $53,655 RI#1215 PHONE: RIPLE N WELL# ok drilled to 11339' squeezed 11235' w/1500 sks cmt 12594' Hadi 2/28/2012 D: 12600'

13 DAE: 3/26/2012 Mond DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 1050 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 4:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. Well on Vac C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Ex-changed service rig arrived on location. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F MI &RU asic rig # 1623, tied guy lines to perm anchors. E- Andrew pump 0 0 Pump repair OP' 100 Cavaloz - RU floor and handling tools, pooh tapered rod string,and stand rods in basket. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Ex-changed tools, and latched on 2-7/8" tubing. Rigged up M vac truck - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I pump 80 bbl water down tubing string and workd tubing loose. Attempt H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J to circulate well, no circulation. Cont'd IH with tubing, tagged junk & solids I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K at 11500'. Continued pumping water to gain circulation, no returns. J- Oneource Vac 0 0 hauled water to rev.pit VAC RUCK 350 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 600 UCKER -M pooh with 60 joints tubing to check fluid level, no fluid level. L- M.Vac trucks hauled water to rev.pit Closed wellbore in. DFN. M- ucker forklift Unloaded work string. Will continue drilling to D of 12599' otal vol of water lost in the hole: 1940 bbl. DAILY CO 4,350 AFE $ ACCIDEN: -0- Daily Cost: $4,350 PREVIO CO 53,655 REPOR Y: Hadi C.Cost $58,005 OAL CO 58,005 $58,005 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt drilled to 11500' 12594' Hadi 2/28/2012 D: 12600'

14 DAE: 3/27/2012 uesday DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3660 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 4:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F rip back in hole with 30 stds work string and mill. agged bridge plug at E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz '. Rotate mill w/ tongs & chased down bridge plug from 11500' ' F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 700 ejas -H ridge plug made a sudden stop going down hole!!. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I Rigged up swivel, mill on bridge plug while pump water at slow rate. Milled H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J 45 minutes no movement. "orque and pipe movement Indicated a tubing I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K stem and/or fish holding Cast Iron ridge Plug from going down". J- Oneource Vac 0 0 hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M Laid down swivel, pooh with tubing to read mill condition. Pulled 218 joints L- M.Vac trucks hauled water to rev.pit of 2-7/8" tubing in clear and closed well in. M- ucker forklift Unloaded work string. We learn that as usual "aker D lockset w/seal section in the hole'!!!! otal vol of water lost in the hole: 1990 bbl. Note: May use a N2/foam unit at a cost near $15000/day. DAILY CO 6,660 AFE $ ACCIDEN: -0- Daily Cost: $6,660 PREVIO CO 58,005 REPOR Y: Hadi C.Cost $64,665 OAL CO 64,665 $64,665 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt cibp cast iron bridge plug to be 5.61" downhole is lookling like this top of fish 12364'!!! 12594' Hadi 2/28/2012 D: 12600'

15 DAE: 3/28/2012 Wed DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3660 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 2100 Hinton -C tart ime:7:am top time: 4:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Finished pooh with tubing and HA, Laid down mill in good condition. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Made up and trip in hole with 5-7/8" shoe on 1 joint of wash pipe on E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz joints of 2-7/8" work string. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 230 ejas -H RU wivel, lowered and tagged at 12370' pipe mmnts. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I gravity feed water and start milling on CIP, made 5". PUIC and closed H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J well in. DFN. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K Will continue J- Oneource Vac 0 0 hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. DAILY CO 6,440 AFE $ ACCIDEN: -0- Daily Cost: $6,440 PREVIO CO 64,665 REPOR Y: Hadi C.Cost $71,105 OAL CO 71,105 $71,105 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt cibp cast iron bridge plug to be 5.61" downhole is lookling like this top of fish 12364'!!! 12594' Hadi 2/28/2012 D: 12600'

16 DAE: 3/29/2012 h DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3660 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 2100 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E Lowered wash pipe, agged bridge plug at 12370'. RU swivel, millover D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F from 12370' to aker Mod D packer at 12380'. lacked off 8k on shoe. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Pooh with tubing string and HA. Checked shoe, OK. No object in the F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Wash pipe. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I Rabbit wash pipe and rip back in hole with 1 joint of wash pipe on set H- ejas Vac rucks huling water to rev pit. VAC RUCK 300 Once ource -J of Oj. Ran 120 joints in the hole and closed well in. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K DFN. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. DAILY CO 6,510 AFE $ ACCIDEN: -0- Daily Cost: $6,510 PREVIO CO 71,105 REPOR Y: Hadi C.Cost $77,615 OAL CO 77,615 $77,615 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt cibp cast iron bridge plug to be 5.61" downhole is lookling like this top of fish 12364'!!! 12594' Hadi 2/28/2012 D: 12600'

17 DAE: 3/30/2012 Frid DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3660 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 2100 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Finished IH with tubing and wash pipe. agged higher at 12370'. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Rigged up wivel, gravity feed water and start milling on bridge plug and F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H fish. Drilled on plug 4 hrs. made 1.5' unable to get back to previous day depth. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I H- ejas Vac rucks huling water to rev pit. VAC RUCK 450 Once ource -J Pulled 10 stands in clear. Closed well in. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K DFN. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M Crew will be off on at and un. L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. DAILY CO 6,660 AFE $ ACCIDEN: -0- Daily Cost: $6,660 PREVIO CO 77,615 REPOR Y: Hadi C.Cost $84,275 OAL CO 84,275 $84,275 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt cibp cast iron bridge plug to be 5.61" downhole is lookling like this top of fish 12364'!!! 12594' Hadi 2/28/2012 D: 12600'

18 DAE: 4/2//2012 Mond DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 2470 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 2100 Hinton -C tart ime:7:am top time: 3:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Finished pooh with work string and HA. Checked shoe and wash pipe, E- Andrew pump 0 0 Pump repair OP' 100 Cavaloz - shoe worn out. end shoe to work on. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H hut down operation due to high wind, and dust storm. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. DAILY CO 5,070 AFE $ ACCIDEN: -0- Daily Cost: $5,070 PREVIO CO 84,275 REPOR Y: Hadi C.Cost $89,345 OAL CO 89,345 $89,345 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt cibp cast iron bridge plug to be 5.61" downhole is lookling like this top of fish 12364'!!! 12594' Hadi 2/28/2012 D: 12600'

19 DAE: 4/3//2012 u DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3500 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 4400 Hinton -C tart ime:7:am top time: 5:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit, mills, shoes PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Checked re-designed shoe, mu and tih with 5-7/8" shoe on 1 jt wash pipe E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - and set of jars. agged fish at 12376'. Ru swivel, milled over 2-3/8" tubing F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H and cont'd to top of aker mod "D" perm packer at 12380'. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I gravity feed water, and cont'd milling over packer at 12380'. Milled over H- ejas Vac rucks huling water to rev pit. VAC RUCK 650 Once ource -J packer 2 hrs,and packer came loose and dropped 5 ft. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K Flushed with water, and start out hole with tubing and HA. Pulled 160 jts J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L in clear and closed well in. K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M DFN. L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. will continue. DAILY CO 9,000 AFE $ ACCIDEN: -0- Daily Cost: $9,000 PREVIO CO 89,345 REPOR Y: Hadi C.Cost $98,345 OAL CO 98,345 $98,345 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt cast iron bridge plug to be 5.61" top of fish 12364'!!! 12594' Hadi 2/28/2012 D: 12600'

20 DAE: 4/4//2012 Wed DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3600 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 6200 Hinton -C tart ime:7:am top time: 7:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit, mills, shoes PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Finished pooh with 2-7/8" work string and HA. Laid down wash pipe E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - and shoe. hoe appears to be in good condition. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Re-dressed 5-3/4" O, w/2-3/8" grap and IH on set of J, OJ, and two - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I dc's on work string. H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J agged 2-3/8" tubing fish at 12369'. Dressed off top of fish 20 minutes using I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K rig tongs. lacked off over fish and engaged fish. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L pulled fish off bottom with 95k, free and start out hole with 4 pts drag. K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M Pulled 142 joints 2-7/8" tubing, and Closed well in. L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. will continue. DAILY CO 10,250 AFE $ ACCIDEN: -0- Daily Cost: $10,250 PREVIO CO 98,345 REPOR Y: Hadi C.Cost $108,595 OAL CO 108,595 $108,595 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt aker lock set w/seal section cast iron bridge plug to be 5.61" top of fish 12364'!!! something like this must be in the hole Hadi 2/28/ ' no rat hole D: 12600' No rat hole.

21 DAE: 4/5//2012 H DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3600 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 4200 Hinton -C tart ime:7:am top time: 7:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit, mills, shoe PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Fin pooh w/ work string and HA, pulled overshot to rig floor. No recovery E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Made up extension and long trip back in hole on 5-3/4" overshot, dc's and F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H jars on work string. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I Eng fish, pull 5' and laid down top joint. tart out hole fish stuck. H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J work and jar 106k. Working and jarring on fish 1.5 hr. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K Closed wellbore in. DFN. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M will continue. L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. DAILY CO 8,250 AFE $ ACCIDEN: -0- Daily Cost: $8,250 PREVIO CO 108,595 REPOR Y: Hadi C.Cost $116,845 OAL CO 116,845 $116,845 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt aker lock set w/seal section cast iron bridge plug to be 5.61" top of fish 12364'!!! something like this must be in the hole Hadi 2/28/ ' no rat hole D: 12600' No rat hole.

22 DAE: 4/6//2012 Frid DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3100 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 5000 Hinton -C tart ime:7:am top time: 4:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit, mills, shoes PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Picked up on tubing 106,000 lb fish still stuck. tart working fish and E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - PU extra joint and jarred down fish free from bad spot. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H pooh with work string and HA, fish dragging up the hole. Fin pooh - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I with 396 joints tubing, and HA. Pulled overshot & fish to rig floor H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J recovered: short 1'cracked 2-3/8" fishing neck, aker MD "D" packer I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K with seal section, and 5 joints of 2-3/8" tubing, and 1 joint 2-3/8" oranged J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L pilled tubing. K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M Minor pices from cast iron flapper valve and rubber elements missing. L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. Laid down fish and Closed wellbore in. DFN. Released rig crew for ood Friday. will resume to clean up wellbore. Fluid level near 4000' DAILY CO 8,550 AFE $ ACCIDEN: -0- Daily Cost: $8,550 PREVIO CO 116,845 REPOR Y: Hadi C.Cost $125,395 OAL CO 125,395 $125,395 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt aker lock set w/seal section cast iron bridge plug to be 5.61" top of fish 12364'!!! something like this must be in the hole Hadi 2/28/ ' no rat hole D: 12600' No rat hole.

23 DAE: 4/9//2012 Mond DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 2800 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 3200 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. mall gas blow C- Hinton provide fishing tools, Reverse unit, mills, shoes PUMP REPAIR 0 Andrew Pump -E D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Re-arranged fishing equipt. IH with Junk mill, 2 dc's and set of jars E- Andrew pump 0 0 Pump repair OP' 100 Cavaloz - and 2 baskets on 2-7/8" work string tubing. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H agged at 12535' (perfs 12500'-). Mill and washed down from - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I 12535' to 12563'. Attempt to circulate, no circulation. Well on vac H- ejas Vac rucks huling water to rev pit. VAC RUCK 800 Once ource -J I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K hut down to repair breaks on the rig for 3 hrs. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L Repair rig breaks, pulled 2 joints in clear, and closed wellbore in. K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M DFN. L- M.Vac trucks hauled water to rev.pit Will continue. M- ucker forklift Unloaded work string. PD 12563' perfs D drilled 12600' Not enough rathole DAILY CO 7,300 AFE $ ACCIDEN: -0- Daily Cost: $7,300 PREVIO CO 125,395 REPOR Y: Hadi C.Cost $132,695 OAL CO 132,695 $132,695 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt aker lock set w/seal section cast iron bridge plug to be 5.61" top of fish 12364'!!! something like this must be in the hole Hadi 2/28/2012 PD 12563' no rat hole D: 12600' No rat hole.

24 DAE: 4/10//2012 U DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3800 asic -A ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 3000 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit, mills, shoes PUMP REPAIR 0 Andrew Pump -E Lowered mill, tagged btm at 12563', no fill over night. ravity fed water D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F and continued milling on packer and bridge part F/12563' to 12580' E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - perfs reported to be at 12500'-. Cleaned up to 40 ft below perforations. F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H displaced 65 bbl water down tubing string, and laid down power swivel. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I H- ejas Vac rucks huling water to rev pit. VAC RUCK 600 Once ource -J Pooh with 2-7/8" work string, and HA. Laid down mill and boots. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K some objects recovered. Will break down tools tomorrow. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M Plan to swab test Ellenberger formation!!! L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. PD 12581' perfs D drilled 12600' DAILY CO 7,850 AFE $ ACCIDEN: -0- Daily Cost: $7,850 PREVIO CO 132,695 REPOR Y: Hadi C.Cost $140,545 OAL CO 140,545 $140,545 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt aker lock set w/seal section something like this must be in the hole not enough rat hole Hadi 4/10/2012 PD 12580' No rat hole. D: 12600'

25 DAE: 4/11//2012 Wed DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE NO.. Pending $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3000 asic -A 11996' ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit, mills, shoe PUMP REPAIR 0 Andrew Pump -E roke off fishing tools, recovered 8 pieces of "D"packer parts & slick line D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F wires. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - Made up and IH with Arrowset 1-x isolation packer on 386 joints of 2-7/8" F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H work string tubing. et packer at 11996' above Ellenberger perforation. - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I Made up swab tools with new rope socket. IH with swab tools, tagged fluid H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J at 3500'. I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K run tag pull %oil J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L ' % K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M ' 0% L- M.Vac trucks hauled water to rev.pit ' 5900' 0% M- ucker forklift Unloaded work string. recovered 14 bbl of &W hut down to work on breaks. Closed well in. DFN. PD 12581' perfs D drilled 12600' DAILY CO 5,300 AFE $ ACCIDEN: -0- Daily Cost: $5,300 PREVIO CO 140,545 REPOR Y: Hadi C.Cost $145,845 OAL CO 145,845 $145,845 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt aker lock set w/seal section something like this must be in the hole not enough rat hole Hadi 4/10/2012 PD 12580' No rat hole. D: 12600'

26 DAE: 4/12/2012 h. DAILY WORKOVER / COMPLEION REPOR IO RIPLE N API# WP RE COUNY AE ANDREW AFE NO. W.I. 100% RO AFE AFE- N $389,000 JO DECRIPION: UPPLEMEN 1 Drill and clean up wellbore to Ellenberger formation 12599'. wab test Ellenberger. OAL RO AFE X IZE W. RADE DEPH HREAD C 13-3/8" 48# H ' &C PERF: D PD PERF ODY CO IEM Estimate $ VENDOR ON-OFF RI 3400 asic -A 11996' ACK HOE 0 JRC - WORK PERFORMED A- asic well service provide service rig REVERE UNI 1850 Hinton -C tart ime:7:am top time: 6:30 pm - JRC dug dirt pit UPERVIOR 400 Hadi -D Opened well, no pressure. C- Hinton provide fishing tools, Reverse unit, mills, shoes PUMP REPAIR 0 Andrew Pump -E IH w/swab tools, tagged fluid at 3400', pulled from 5400'. D- Hadi supervise operation & fishing Dope and valve 0 Produ. pecial -F Made 20 swab runs pulling from 8300'. Fluid rising 500 to 700' per run. E- Andrew pump 0 0 Pump repair OP' 50 Cavaloz - F- Prod. pecialty 0 0 Pipe dope, valves, wood seals VAC RUCK 0 ejas -H Note: on 15th swab run, crew changed tools for un-known reasons and - Cavaloz provide bop stack. WIRE Line 0 Rotary wl -I trip in hole. pooh with no fluid. wab cups and mandrel left in tubing. H- ejas Vac rucks huling water to rev pit. VAC RUCK 0 Once ource -J Continued swabbing. Made 20 swab runs,pulling fluid from 8300' I- Rotary wire line tand by to cut pipe. 2-7/8" U 0 DRM -K Recovered 104 bbl of water and trace of oil. Closed well in. J- Oneource Vac hauled water to rev.pit VAC RUCK 0 M.VAC -L DFN K- DRM pipe co /8" tubing FORK LIF 0 UCKER -M Will continue swabbing well. L- M.Vac trucks hauled water to rev.pit M- ucker forklift Unloaded work string. PD 12581' perfs D drilled 12600' DAILY CO 5,700 AFE $ ACCIDEN: -0- Daily Cost: $5,700 PREVIO CO 145,845 REPOR Y: Hadi C.Cost $151,545 OAL CO 151,545 $151,545 RI#1623 asic PHONE: RIPLE N WELL# ok squeezed 11235' w/1500 sks cmt not enough rat hole Hadi 4/10/2012 PD 12580' D: 12600'

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